ANALISIS RESETTING RELE JARAK AKIBAT UPRATING KONDUKTOR GIS PESANGGARAN - GI SANUR

Main Authors: Akbar Fauzany, Rizal, Dyana Arjana, I Gede, Indra Partha, Cok Gede
Format: Article info application/pdf eJournal
Bahasa: eng
Terbitan: Program Studi Teknik Elektro UNUD , 2019
Online Access: https://ojs.unud.ac.id/index.php/spektrum/article/view/49776
https://ojs.unud.ac.id/index.php/spektrum/article/view/49776/29569
Daftar Isi:
  • Increased load current on the Pesanggaran – Sanur transmission line by 333,536 Ampere or 83,384 % of the current carrying capacity caused the uprating conductor from ACSR Partridge 135 ????????2 into ACCC Lisbon 310 ????????2. Upratingj cause changes in impendance value. This change affects the zone reach protection of GIS Pesanggaran – GI Sanur distance relay which overlaps with Zone protection of GI Sanur – GI Gianyar distance relay. Resetting is done by recalculation according the distance relay rules and the result are tested with short circuit at 86 % Pesangaran – Sanur transmission line. Resetting result shows the distance relay operate appropriately according with the IEEE Standard C37.113-2015.